New Method for Die Casting of Automotive Components Saves Energy and Material
Submitting Institution
Queen's University BelfastUnit of Assessment
Aeronautical, Mechanical, Chemical and Manufacturing EngineeringSummary Impact Type
TechnologicalResearch Subject Area(s)
Information and Computing Sciences: Artificial Intelligence and Image Processing
Engineering: Materials Engineering
Summary of the impact
Die Casting is one of the most widely used production processes for
aluminium automotive components with examples including engine blocks and
gear-box casings. Ryobi Ltd is the world's leading die casting
manufacturer.
Researchers at QUB have developed a modified casting process with an
optimised start-up procedure. Ryobi has implemented the new method across
its entire UK facility's die casting machines resulting in total
yearly savings of approximately £1,000,000, 742 GJ energy (enough to
power 50 domestic homes) and nearly 60 tonnes of aluminium. This
demonstrates clear economic and environmental benefits, which have further
potential for global impact.
Underpinning research
Ryobi approached Queen's university for help in 2000 as they wished to
gain a better understanding of die heat check cracking (low-cycle fatigue
failure) with the objective of extending die life. At that time, the
university had limited expertise in this area. Dr Thornhill took the
lead in establishing a research program with Ryobi. Prior to
academia he had been a designer in industry and had extensive experience
of designing cast components and working with aluminium alloy foundries on
new products and troubleshooting existing ones. Professor Armstrong
provided valuable support through his expertise in numerical simulation.
He has an international reputation for his work in computer aided
engineering and in particular finite element analysis. He was also
co-author of the standard undergraduate text "Mechanics of Engineering
Materials".
Initial experimental research was carried out by Makoto Kurokawa, Ryobi
plant manager, under the guidance of Thornhill and Armstrong. It was
clear, however, that to make real progress a dedicated research associate
was required. With funding from INI and Ryobi, Alastair Long joined the
team in 2005. Long was a graduate of Queen's University but subsequent to
his degree had spent six years in industry with another large foundry,
Montupet, gaining significant expertise in computer simulation of the
casting process.
A thermal fatigue test rig, designed by Thornhill and developed by Long,
demonstrated that the dominant cause of die failure was the difference in
temperature between the high point in the cycle and the low point.
Computer simulation of the casting process using MAGMA casting simulation
software predicted that the temperature differences were greatest when a
die is first put into operation [1,2]. This was validated by instrumented
production dies with thermocouples implanted close to the dies surface and
strain gauges in pockets machined into the back of the die. It was
demonstrated that it could take between twelve and fifteen casting cycles
for the process to normalise and the corresponding fatigue loading to
minimise [3,4].
David Watson took over as Ryobi plant manager in 2007 and facilitated
experimental work on a production casting machine that allowed Long to
reduce the number of casting start-up cycles before the process normalises
down to as few as five by management of the die cooling system during this
crucial period [5].
References to the research
Research outputs
1. Investigation of thermally induced die cracking for H13 High Pressure
Casting dies using simulation methods. Long, Alastair; Thornhill, David;
Armstrong, Cecil; Kurokawa, Makoto; Hendry, Arthur. Society of Automotive
Engineers, 2007-31-0100.
2. *Determination of the heat transfer coefficient at the metal-die
interface for high pressure die cast AlSi9Cu3Fe. Long, Alastair;
Thornhill, David; Armstrong, Cecil; Watson, D. Applied Thermal Engineering
, Vol. 31, 12.2011, p. 3996-4006. DOI:
10.1016/j.applthermaleng.2011.07.052
3. *Predicting die life from die temperature for high pressure dies
casting. Long, Alastair; Thornhill, David; Armstrong, Cecil; Watson,
David. Applied Thermal Engineering , Vol. 44, 2012, p. 100-107. ISSN:
1359-4311. DOI: 10.1016/j.applthermaleng.2012.03.045.
4. Stress correlation between instrumentation and simulation analysis of
the die for high pressure die casting. Thornhill, David; Long, Alastair;
Armstrong, Cecil; Watson, David. International Journal of Metalcasting ,
Vol. 7, No. 2, 2013, p. 27-41.
5. *The Impact of Die Start-Up Procedure for High Pressure Die Casting,
Long, A., Thornhill, D., Armstrong, C., Watson, D., SAE Int. J. Mater.
Manf. 6(3):2013, DOI: 10.4271/2013-01-0829
*Best three outputs
Grants
• Original project (11/10/2005):
Extending die life of high pressure die casting dies, £1220k project,
£418k to QUB (Thornhill, D; Armstrong, C), Direct industrial finding-
Ryobi
• Follow up project (19/10/2010):
Reducing part cost of aluminium die castings by minimising gate size,
£1541k, £434k to QUB (Thornhill, D; Armstrong, C), Direct industrial
finding-Ryobi
Details of the impact
The collaboration between Ryobi Aluminium Casting and QUB has enabled the
company to develop knowledge and expertise in new areas which will have
long-term benefits. John Hughes, managing director of Ryobi Aluminium
Casting has stated "The enhancements we've made to our processes as
a result of this research and development project have not only
created cost savings but put us in a stronger, more competitive
position to target higher volume and longer term projects across
Europe."
The extension to die life due to managing the thermally induced low cycle
fatigue through die start up is between 20% and 50%. This manifests itself
as less frequent die repair and a longer overall die life before it is
considered non-viable. The reduced frequency of die repair will directly
impact the overall equipment efficiency (OEE) of the die casting machine,
though this will also be influenced by reducing the number of scrap
castings.
As castings produced during die warm up are of inferior quality they are
scrapped. The revised start-up procedure reduces the number of
castings scrapped by as many as ten castings per die start up.
Although scrap castings are recycled, each time the metal is remelted up
to 8% of the material is lost as it oxidises and forms dross.
Additionally, it takes approximately 1 MJ/kg to melt aluminium so there is
a significant energy saving from remelting less scrap castings.
The revised start-up cycle was tested at the start of June 2009
resulting in an immediate impact on scrap and the overall equipment
efficiency (OEE) of the casting machine. The impact on production before
and after its introduction is illustrated in Table 1.
Table 1, Summary of the changes due to the modified die start-up.
|
OEE %
|
Scrap %
|
Parts cast
|
Part cost
|
Jan – April 09 |
66.62 |
11.5 |
34,871 |
£5.22 |
June – Oct 09 |
74.59 |
7 |
43,711 |
£4.57 |
The casting used for illustration in Table 1 has a production cycle time
of 75 seconds and a production volume of 250,000 parts per year, on two
casting machines. Therefore the saving due to the reduction in part
cost alone is equivalent to £81,250 per year per casting machine.
The 4.5% reduced scrap rate increases the number of good castings that
can be produced from the die within its normal working life. As a typical
die life, before it is considered uneconomical to repair, is 100,000 parts
and the manufacturing cost is of the order of £200,000 this represents an
additional saving per year per casting machine of £13,675. This does
not include savings made by extending the die life due to reducing the
thermally induced fatigue stress.
The shot weight per casting is approximately 12kg. As there is 4.5% less
scrap this represents 67.5 tonnes of metal per casting machine per year
that isn't remelted, saving 67.5 GJ of energy and potentially 5.4 tonnes
of material saved due to reduced dross loss.
Since 2009, Ryobi has rolled out the new casting start-up method across
the Carrickfergus factory's eleven die casting machines. Assuming
similar savings on all casting machines, this represents total savings
of approximately £1,000,000 per year, 742 GJ energy saving and nearly 60
tonnes of aluminium alloy not reduced to dross. At the same time
there is a small but useful increase in factory capacity due to the
increased OEE.
Sources to corroborate the impact
- Belfast Telegraph Newspaper article (10th July 2013):
http://www.belfasttelegraph.co.uk/business/business-news/japanese-companys-links-with-queens-university-pays-off-29408160.html
- Plant Manager
RYOBI Aluminium Casting (UK) Limited, Carrickfergus
- SAE Paper 2013, The Impact of Die Start-Up Procedure for High Pressure
Die Casting (joint QUB/Ryobi publication http://papers.sae.org/2013-01-0829/
- Invest NI press release (9th July 2013):
http://www.investni.com/newsstory.htm?newsid=18246